quick update, realized i haven’t updated this in a while. july 25th: i figured out my jetting issue was timing, my distributor slipped and it had 12* total, i’m surprised it even ran. also trans gave up transmission: i blew up my 4l60(700r4) which wasn’t shocking just disappointing, i was hoping it would last longer. fully disassembled and everything flushed ect, it burned the forward clutch and the band, and the lower planetary gear set was junk. upgrades coming: .500 boost valve, hardened sunshell, wide band, new frictions, unbreakable pump rings, 13vane pump, 2-3 shift kit and full manual valve body, and i’m gonna go for a 3500stall torque converter, just give it a little more jump off the line i also 3d printed a carb spacer, after i get it running consistently i plan on porting the intake, and building a custom header for the driver side, i can 3d print 1” sections that snap together and have angles ect to model it before i cut and weld stuff, but that’s after i’ve driven the car for a bit cuz i needa drive this damn car school has crushed me these past couple of months so i ain’t been able to work on the car like i’ve wanted, but when i get it back together i’m gonna be the fastest car at the school Sent from my iPhone using Tapatalk